As you all know, Coffee (Dean) passed away a couple of years ago. I am Dean's ex-wife's husband and happen to have spent my career in tech. Over the years, I occasionally helped Dean with various tech issues.
When he passed, I worked with his kids to gather the necessary credentials to keep this site running. Since then (and for however long they worked with Coffee), Woodschick and Dirtdame have been maintaining the site and covering the costs. Without their hard work and financial support, CafeHusky would have been lost.
Over the past couple of weeks, I’ve been working to migrate the site to a free cloud compute instance so that Woodschick and Dirtdame no longer have to fund it. At the same time, I’ve updated the site to a current version of XenForo (the discussion software it runs on). The previous version was outdated and no longer supported.
Unfortunately, the new software version doesn’t support importing the old site’s styles, so for now, you’ll see the XenForo default style. This may change over time.
Coffee didn’t document the work he did on the site, so I’ve been digging through the old setup to understand how everything was running. There may still be things I’ve missed. One known issue is that email functionality is not yet working on the new site, but I hope to resolve this over time.
Thanks for your patience and support!
hey tinken i matched the large brass screw with my 449, 5 and a quarter turns out from all the way in. did the tps battery disconnect hoping this fixes it. if i turn out the screw it does idle a little faster but the throttle starts to hang up like it wont un rev. i have fmf and map 3 on both bikes 449 runs great no issues but 511 started stalling at about 500 miles no issues til the 500 mile mark. no mods to airbox, so turning out the screw adds more air which i found makes it stall worse. more air less fuel too lean correct? turning in the screw should fatten it up right? will that solve it, or am i destined for a PCV.
Mods are, fmf no insert, jumper in, map 3. 2 1/4 turns lowers the idle to much and stalls. If i open the screw anymore it sounds like its sucking way to much air and stalls. The bike has 570 miles on it, doing the battery disconnect and matching the 449 seemed to help but not eliminate the stalls. gonna do oil changes this weekend and ride it to see if its still doing it, weather permitting. I did the disconnect and screw adjustment about a week and a half ago and rode it after that with only a couple stalls (better than before). other than stalling it freakin rips.....thxIsn't 5 1/4 turns about three turns too many? I think the advice is to go 2 1/4 or 2 1/2 and adjust +/- 1/8 turn from there??
Mods are, fmf no insert, jumper in, map 3. 2 1/4 turns lowers the idle to much and stalls. If i open the screw anymore it sounds like its sucking way to much air and stalls. The bike has 570 miles on it, doing the battery disconnect and matching the 449 seemed to help but not eliminate the stalls. gonna do oil changes this weekend and ride it to see if its still doing it, weather permitting. I did the disconnect and screw adjustment about a week and a half ago and rode it after that with only a couple stalls (better than before). other than stalling it freakin rips.....thx
I believe so. Also, install Q-insert.(Tinken can he swap them?).
yes sir gonna check filter, change oil, adjust chain, put the insert in that came with the fmf pipe and turn screw in a quarter turn at a time and see if it helps...great idea switching ECU's didnt even think of that...Due to it being ridden on the street as a motard and only having 570 miles I havent even had air filter out of it yet LOLClean and lightly oil your air filter. Make sure it isn't torn. And make sure its good and oiled where it makes contact with the airbox. Then maybe swap your ECUs to make sure you don't have a computer issue. (Tinken can he swap them?).
https://www.denniskirk.com/fmf/powercore-4-quiet-core-insert.p435531.prd/435531.skuTinken, by quiet insert on the fmf do you mean the normal spark arrestor end cap? Or do you mean the quiet powercore 4 insert, or do you mean the fmf q4 insert (most restrictive) which adds the most power? I will try whichever you recommend. It is deceiving with the noise increase.
I like this and is what I did as well. The Zipty Factory maps are created by Ty and do not have this, but when I created the Burson map, I added something similar.So far seems okay. I did add the same amount of fuel to correct idle afr (about 8 at 1750 and 5 at 2000, 3 at 2200) and copied that to the map to the right (0, 5, 10) then told auto tune to sort out from 20% on up.
SO, I have made it run more rich at very slight throttle openings at low rpm just off idle. Allowed more air to bypass. Set proper idle AFR. So far no problems but have not had many miles on it.
This is incorrect. The air bypass has nothing to do with increasing/decreasing fuel or mixture ratios. It simply allows more air to pass which is seen by the air flow sensor and more fuel is added to compensate. If a lean condition is occurring, then the air flow sensor may not be picking up on the added air flow and adjusting fuel in the powercommander will alleviate the issue.I can tell you that when you allow more air to bypass it will run LEANER at idle. It directly affects the idle mixture.
When you talk about quite a while what do you mean engine hours? Mileage? What is a good reference?