Wow Dave, sorry to hear that. Where the hell do you get a head gasket for this beast? Halls maybe?
Let me answer that first. I called Cometic and they think they can make a custom one--thicker to lower compression-- for around 60 bucks. He is checking to see if they have the setup to do so, he thinks so.
Since yesterday I have been on the phone looking for piston etc also.
Was thinking to get a BMW piston to drop down to 11:1
I have been racking my brains on this.
What my bike has in common with Quirkey's is aftermarket exhaust and pod mod. I was careful not to alter the flow of the exhaust too much, as in some cases that can cause problems with the heads and valves. I run a single can with restrictor/baffle/spark arrestor. I do believe I flow better than stock, and ecu is supposed to adjust for that. Also have the Brisk plugs.
I did not have pinging on acceleration, but the bike did seem to be louder at idle yesterday, can't swear by it, I wear ear plugs. And today without ear plugs still sounds as usual. Might be that running on the warm side changed the tone.
I just got back from purging the waterless and running straight water, and the temps dropped back to where they should be.
It took longer to reach fan kick on with water, and the bike was already warm from purging the waterless. Once fan kicked on, temps dropped and fan cut off. Fan never cut off yesterday or today with the waterless, even babying at speed.
The waterless I pulled today has a blackish tinge and there are black pieces in it, not many, most 1/8 inch and smaller, pieces. What and where that came from I do not know, but I am thinking about my black rear brake reservoir fluid.
I'm going to let it cool, put regular coolant back in and check it. I will also take the waterless to a rad shop to have tested for exhaust gas. I'm keeping my fingers crossed, the bike still runs great at this moment in time.
One thought is that with the waterless, it may not burp out like the regular coolant as it does not expand. When I changed it, I made sure I got every bit of air I could out, ran it and did it all again. If this is the case, maybe the tiny air bubbles were remaining air bubble that could not burp out proper. And I even tried that yesterday when I tried topping it off and noticed the bubbles.
I did not have any cooling or driving issues prior to the waterless coolant experiment.
Keeping my fingers crossed
