As you all know, Coffee (Dean) passed away a couple of years ago. I am Dean's ex-wife's husband and happen to have spent my career in tech. Over the years, I occasionally helped Dean with various tech issues.
When he passed, I worked with his kids to gather the necessary credentials to keep this site running. Since then (and for however long they worked with Coffee), Woodschick and Dirtdame have been maintaining the site and covering the costs. Without their hard work and financial support, CafeHusky would have been lost.
Over the past couple of weeks, I’ve been working to migrate the site to a free cloud compute instance so that Woodschick and Dirtdame no longer have to fund it. At the same time, I’ve updated the site to a current version of XenForo (the discussion software it runs on). The previous version was outdated and no longer supported.
Unfortunately, the new software version doesn’t support importing the old site’s styles, so for now, you’ll see the XenForo default style. This may change over time.
Coffee didn’t document the work he did on the site, so I’ve been digging through the old setup to understand how everything was running. There may still be things I’ve missed. One known issue is that email functionality is not yet working on the new site, but I hope to resolve this over time.
Thanks for your patience and support!
How much? I cannot find any online.I have a 2010 throttle body with less than 1000 miles
I can part with if you need one
What are the symptoms, why is bike at the dealer?
Still in the shop. New throttle body was put on and it started, but would not start a second time. Dealer stumped and wants to open the motor. I am losing faith.
Just wondering if the ecu fixed your problem? I have a 2010 txc 250 and I was having the same issue with no tps sensor signal but also low voltage error. I also put a throttle body on it with no luck, it would run for about 3 to 7 seconds than die out like running out of gas. New fuel pump and filter and still no luck. Finally took out the wire harness today and unwrapped the entire harness and found two bad wire that rubbed thru with a few strands left. Repaired wires rewrapped harness and put back in and runs like a new bike again.