As you all know, Coffee (Dean) passed away a couple of years ago. I am Dean's ex-wife's husband and happen to have spent my career in tech. Over the years, I occasionally helped Dean with various tech issues.
When he passed, I worked with his kids to gather the necessary credentials to keep this site running. Since then (and for however long they worked with Coffee), Woodschick and Dirtdame have been maintaining the site and covering the costs. Without their hard work and financial support, CafeHusky would have been lost.
Over the past couple of weeks, I’ve been working to migrate the site to a free cloud compute instance so that Woodschick and Dirtdame no longer have to fund it. At the same time, I’ve updated the site to a current version of XenForo (the discussion software it runs on). The previous version was outdated and no longer supported.
Unfortunately, the new software version doesn’t support importing the old site’s styles, so for now, you’ll see the XenForo default style. This may change over time.
Coffee didn’t document the work he did on the site, so I’ve been digging through the old setup to understand how everything was running. There may still be things I’ve missed. One known issue is that email functionality is not yet working on the new site, but I hope to resolve this over time.
Thanks for your patience and support!
Well, I have plenty of bills too. I ride to help me forget about them!Dirtdame;22603 said:Congratulations. The only things that ever seem to follow me home are bills.![]()
krieg;22604 said:Well, I have plenty of bills too. I ride to help me forget about them!![]()
krieg;22758 said:RIDE REPORT:
The other difference I noticed between the 125 and the 300 was the fact that the 300 is just heavy enough to keep things planted when things got bouncy. The 125's front wheel tends to get wild and bounce around in the choppy stuff (choppy stuff meaning ruts and rocks and roots... not whoops or typical MX track stuff).
The engine likes to vibrate. Although, in fairness, as it broke in throughout the day things got a bit smoother.
I think the pilot jet may be a tad rich as the engine had the slightest burble immediately coming off closed throttle.
Rusty 2;22795 said:Check your engine mount bolts for proper torque.
Same exact thing with mine! It was spot-on perfect back when it was colder around here,...but now that it's hitting 70* for daytime highs I've got the burble right at the first crack of the throttle too. What pilot jet do we need? I tried opening the air screw a half turn,...that worked (somewhat) at 50-60 degrees,...but above 70* it's obvious the pilot is just too fat.
I get some crazy conflicting info when reading about the jetting. By some reports we have a 400 main and a 35 pilot,...but I've also seen 380 main and 17.5 pilot...? Then again there's supposedly a limited power version of our bike that's street legal in Europe, so maybe that's getting mixed up in there too.
I'd just like to have the right assortment of jets on hand before I crack the carb open,...know what I mean?
My bike blows black spooge all over my rear fender and it runs down the silencer housing,...with the fat pilot, and 32:1 ratio, at 70*+ temps.
Does yours? Will switching to 40:1 after break-in help any?
I had a coolant leak too. Not at the head, but down where that big weirdo hose that comes off the bottom of the radiators connects to the water pump cover. I tried tightening the clamp, but I must've cut through the inner wall of the hose, because now it seeps through the "fiber pockets" in the cross section of the end of the hose.Got a new one on the way from Hall's.
What did you put back in your bike for coolant after you torqued the head bolt and stopped the leak?
Well, I gotta get off here and call Upstate Cycles about those frame guards now,...wish me luck.![]()
No way do I think you're acting like a know-it-all! I appreciate you taking the time to offer suggestions based on your experiences. Thanks!PC.;22799 said:Going from a 32:1 to a 40:1 mixture will actually richen your jetting (less oil molecules = more gas molecules in the mixture). More gas in the mix = less air in mix = richer jetting. It may reduce the amount of spooge dripping from the silencer, but at the cost of reduced lubrication to the crank and potentially ring seal and life. Always jet for your mixture and never alter your mixture for the jetting. With that said, I run Klotz R50 32:1 in all my strokes and jet for that mix only.
The problem is your combustion chamber is not getting hot enough for a complete burn of the gas/oil mixture. The chamber is hot enough to burn the raw fuel, but leaves the oil behind and sends it out the exhaust ports as spooge. Got to get that chamber burning hotter.
You've got a few options as I see it.
-Reduce the amount of fuel mix vs. air entering the chamber via smaller jets. Works great up to a certain point, but the consequences can be bad (lean seizure, detonation)
-Run a hotter plug. A band aid fix IMO and can lead to excessive heat damage on the piston.
-Tighten the squish in the head. The real fix IMO. These are mass produced machines with semi-tight tolerances. An optimal squish clearance (between the piston crown at TDC and the edge of the combustion chamber) is subject for debate as a race motor that will never have a worn bottom end can get away with .025" or less squish. Our trail motors may go hundreds of hours without a bottom end rebuild, so we do not want to walk the line so tightly and risk the piston hitting the head as the crank bearings wear. I run my motors at .045" squish and have the dome machined to bring it back to stock compression.
I cant speak on the Husky (as I haven't even ridden it yet), but I have lots of experience with this on Yamaha YZ's. When my 06' yz250 was bone stock it would spooge no matter what. I mean it.... going from 32:1 to 40:1 had no impact. Leaning out the power jet, pilot, needle had no effect. Once the head was cut from .062" down to 0.45" it was gone. Immediately. The head and its loose tolerance was not allowing for a complete burn in the dome. After that, I could jet it spot on every time and the throttle response went from good to excellent. Best $70 I've spent, bar none.
Once I get the 300 broken in and some seat time I'll take a squish reading and see where it is. I'm guessing its going to be on the loose side and the squish work will be of great benefit. It's all speculation at this point, but I've yet to see any mass produced engine within an acceptable range.
Hope you enjoyed my thesis. I dont mean to sound like a know-it-all (which I'm certainly not), but I do have some knowledge with 2 stroke building and jetting and everything I've stated is based upon my personal experience. Take it for what it's worth.
-PC
Hope you enjoyed my thesis. I dont mean to sound like a know-it-all (which I'm certainly not), but I do have some knowledge with 2 stroke building and jetting and everything I've stated is based upon my personal experience. Take it for what it's worth.
-PC