1982 XC 430
Husqvarna
AA Class
Anybody ever see one like this ? Looks like the Liner Cracked all the way around at the transfer ports and then the loose parts made there way up the Transfer Ports. This Motor had about 2 hrs running time on it since I went threw it. This is the 1984 AC 250 with all the extra Ports. I had Port Matched and cleaned them all up but I had never removed the Liner. When I bought the project it had the original rear Tire, and Piston. And yes the Rod lower end is shot to. This bike was running great and ( look at the spark plug color ) I was just ripping down the back straight. You would think that there was a big bang when this happened but it acted like it ran out of gas I used the kill button to shut it off. It wasn't till I realised the kick start was froze before I suspected any thing was wrong.